
DETAILED
STUDY
As part of the sites
environmental policy a study was conducted by The Humber Resource Efficiency
Centre to ascertain whether we were managing our production of waste materials
so as to have the minimum impact on the environment,and having produced
the waste were we fully conversant with all the various methods of disposal.
As dross formed a
large part of our waste material it was decided to measure the impact
of the Solder Recovery System on our waste levels.
The recovery system
was used on one of our three solder machines so that a comparison between
solder usage with and without the EVS could easily be made. The trial
was run over a period of one month and the figures collected were:
- New solder added
- Weight of recovered
solder
- Weight of waste
dross
- Number of boards
soldered
For the purpose of
the results, machine 1 used the EVS.
OPERATION
The operating of
the EVS is very simple and basically consists of adding hot or cold dross
into a heated chamber,compressing the dross with a heated piston,collecting
the usable solder squeezed out in an ingot tray and at the end of the
cycle discharging the waste dross down a chute directly into a bin for
disposal. Maintenance is minimal and easy and each unit has the ability
via supplied software to monitor the machine operation and feedback any
fault details.
In our experience
it was found that a better return was achieved when small amounts of dross
were processed often rather than one or two large amounts. No major problems
have been encountered with the machine and all of our minor problems have
been addressed by the manufacturers and remedial improvements incorporated
into their latest machines. Spares, technical back-up and support were
also of a high standard.
RESULTS
Results were collected
and collated on a daily basis but for the purposes of this report they
have been totalled and averaged.
|
Machine
1 |
Machine
2 |
Machine
3 |
| New
solder added |
420kg |
430kg |
212kg |
| Recovered
solder |
232kg |
0 |
0 |
| Dross |
159kg |
273kg |
98kg |
| Boards
soldered |
29,272 |
16,938 |
7,510 |
| Ave
% solder recovered |
59% |
0 |
0 |
| Solder/board |
0.0143kg |
0.025kg |
0.028kg
|
CONCLUSIONS
As can be seen from
the above results a number of different conclusions can be reached. We
were particularly interested in:
- recovery
rate
- saving on solder
usage
The average recovery
rate was 59%,the highest achieved was 79% and the lowest 31%. This difference
can be explained due to two main factors.
- As was mentioned
earlier in the report,the greater the amount of dross loaded into the
machine for processing in general produced a lower return in terms of
reusable solder.
- It is also possible
to process the dross more than once to extract solder so therefore it
is...
- obvious that the
higher the solder content the higher the return,the reverse also holds
true. It would therefore appear that the sample that produced the 31%
return was very low in solder content. The experience of the operators
can also,when combined with the above mentioned factors affect the results
and during this study period a number of new and different operators
were collecting the results.
For the reduction
in solder usage the following calculation was used:
______recycled
solder_______ x 100 = 35.5%
recycled solder + new solder
These figures are
not that far removed from the manufacturers claims and we are confident
that higher returns can be achieved.
The immediate effect
can be seen from the table above,the solder machine with the SRS averages
·0143 kg/brd whereas with the other two machines the average is
·0265 kg/brd a difference of ·0122 kg/brd. This
difference is purely the amount of usable solder being thrown away with
the dross. In this instance
it equates to putting 80% more solder / board.
If we could recover
all of the usable solder in our dross then the returns and hence savings
would be higher than those achieved during the trial period and
could even surpass the manufacturers claims.
If we then also project
using the figures achieved on machine 1 we would have recovered a further
378 kg from machines 2 and 3. This would have
given us a total of 610 kg recovered solder in one month.
If we then assume
the same levels of production for the year we would expect to recover
7,320 kg of usable solder. Based
on £4.54/kg this would give an annual saving of £33,232.
|